Lots of good news. A bit of mind fog on my part though kept today's session from being perfect.
Started pulling one of the two swing-arm bearings into place selecting the side that had suffered the most over the years and the necessary, but brutal disassembly process. I decided to use the axle as the threaded puller, figuring its made of high-grade steel and has a tight thread pattern, making each movement more precise. Good Idea. Another good idea was coating the bearing's outer skin with Permatex, Anti-Seize compound.
I'm slowly cranking the bearing in place. Things were going so well, I forgot that axle had a limited number of threads, so when the going got tough (the axle nut had grounded out), I just thought that it was a bit of deformation down in the swinger's cavity. So, I broke out my trusty breaker-bar and laid into it. No joy. Broke out the heat gun. Still nothing moved. About this time, I tapped on the end of the axle nearest to the bearing and it and the bearing budged a bit. A very dim light bulb goes of in my head.
Now, I had realized what dumb-ass means.
Tried to remove the axle lock nut to take the puller apart and just tap home the bearing. "Nothing is ever fucking easy". It took Kroil, a propane torch and breaker bar to release the lock nut. I believe the threads on the nut are now damaged, as removing it took way to much effort. The bolt threads are OK.
Back to the good news. It was now easy to tap the bearing home using a thin washer and a 22mm socket. Job done. So was I.
On the other side, I'm going to use the same puller rig, get the bearing squared away about half way into the cavity, tear the puller apart, heat the swinger and tap the bearing in place with the washer/socket.
Yamaha is to be commended for their 30 year-old casting technology. My swinger has taken a real beating and is still rock-solid.
PS - I'll be acquiring a tight threaded rod from my bearing guys, soon.